Student Robotics: Working on a Fix

We have decided to disassemble the bot again to replace some parts in order to fix the problem with the turning moment of the motors. Your chance to get a closer look on some of our parts:

In the video below you can see that the wheels are at least moving, but to know if we could really fix the problem, we’ll have to put everything back together and start some tests, on which we are already working!

The good news: We are working on a solution right now. And the solution looks very promising. Stay tuned for another update very soon!

(author: Yannick)

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