This week not everything went as we hoped. For example, we hoped our bot would drive through the test maze with not many problems, but one infrared sensor didn’t work, because the hole was too small. So we fixed that issue. But the next problem was, that we couldn’t test again in school, because one of us got ill. But we had time to mount our battery, so that it doesn’t just lay on top of our bot, and our emergency stop button. We’re looking forward to test next week, and there’s much hope that we can do it at the final competition.